RE: Sol results9 Jul 2019 12:27
If I can only find it, I recall Loto-1 results were affected by a poor cement job. Oh, here we go .....
Part I "The first of two exploration wells, Kamal-1X, was spudded on October 29, 2012, and reached a total measured depth (“MD”) of 10,500 feet in December 2012. Of the multiple sands targeted, the primary target of the Mirador zone encountered a net pay of 20 feet. This zone was tested and yielded a peak rate of 210 bopd of 14? API with high water cut. This test confirmed oil production and mobility and a notice of discovery was filed with the ANH by the operator. However, rates were deemed non-commercial and the operator was directed to abandon the well by the ANH, which was done in mid-February 2014. A 3D seismic program is planned over the Kamal area to enhance clarity and will be used to re-evaluate the Kamal structure.
The second exploration well, Loto-1X, spudded on January 22, 2013, and was drilled to a total depth of 10,500 feet MD. This well targeted the Mirador, Guadalupe and Une sands. Petrophysical evaluation, supported by conventional cores and cuttings descriptions, indicated that the Une, Guadalupe and Mirador reservoir sands were all oil charged, with the Mirador being of the most interest with a petrophysical evaluation showing a high quality net pay of over approximately 65 feet. The testing of the Une zone resulted in extra heavy oil in non-commercial quantities and further testing was abandoned.....
{see part II}