RE: Well file14 Feb 2023 12:21
Seeikinvalue, from first hydrocarbons rns at 16-2, proof that the test was choked/facility constrained, so not all to do with salt Intrusion. Hopefully the new infrastructure in place for the second test has mitigated any salt issue.
State 16-2LN-CC well update overview
· The State 16-2LN-CC well was put on flowback on 28 October 2021, under a heavy 7/64 inch choke in order to prevent formation damage during early stages of flowback;
· The well is now successfully flowing hydrocarbons;
· Although production rates are facility constrained at present, the well is demonstrating highly encouraging daily average flow rates of 420 barrels of oil equivalent per day ("boepd") with recent hourly rates of over 690 boepd on a slightly less restricted 12/64 inch choke setting;
· In addition to hydrocarbons, the well continues to flowback completion fluids at approximately 1,200 barrels per day and production testing remains ongoing:
o Fluid composition is evolving as additional completion fluid is recovered, with ultimate expected gas/oil ratios yet to be determined.
· The well has demonstrated limited pressure drawdown to date despite the high liquid rate, an additional encouraging sign which may indicate a large connected volume.
· Results to date suggest the State 16-2LN-CC is a successful proof of concept well with highly positive implications for the utilisation of hydraulic stimulation completions across the multiple reservoir zones and across the Company's 37,613-acre lease position within the Paradox Basin.