RE: Positive RNS18 Sep 2020 08:34
Following a long delay during the period under review work has resumed to attempt to stimulate the well to flow at rates nearer the 3,800 barrel per day experienced for a brief period in November 2017. A conventional acid treatment has resulted in oil flowing to the surface but not yet at the rates previously encountered
Could mean anything from 1 b to 3799 bs kept in the dark still.