RE: Thatβs the packers removed - well done SYN20 Jul 2023 11:21
They stated "The revised program calls for the removal of the production tubing and milling out of the bridge plug that currently isolates the original four fracked zones from the two currently producing re-frac zones. The production tubing will be re-inserted and per the DGH request, the well will be flowed for a period to establish a baseline of production without artificial lift."
So the "removal of the production tubing" has taken place in last 5 days, so on to
1) Milling out of the bridge plug that currently isolates the original four fracked zones from the two currently producing re-frac zones.
2) The production tubing will be re-inserted and per the DGH request
3) The well will be flowed for a period to establish a baseline of production without artificial lift.
4) During the period of baseline establishment, the workover rig will be deployed to the nearby C-19z oilwell to conduct a de-waxing operation lasting approximately 5 days.
5) Following the C-19z workover, the rig will return to the C-77H well to install the jet pump.
May be the case but not sure we going to hit Gordon's w/c 7th August.