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Update - Riverbend Project, onshore Texas, USA

10 Feb 2011 12:27

RNS Number : 0303B
Empyrean Energy PLC
10 February 2011
 

10 February 2011

 

 

Empyrean Energy PLC

('Empyrean' or the 'Company', (EME))

 

Riverbend Project, onshore Texas, USA

 

 

Empyrean Energy Plc provides the following update on operations at the Riverbend Project in Texas:

 

 

Cartwright-1H well

 

Empyrean has been advised by the operator that a coiled tubing unit was brought in to carry out a cleanout operation on the Cartwright-1H well. During a routine milling operation using the coiled tubing unit prior to the cleanout operation the mill tagged up on an obstruction in the hole at 13,641' measured depth. The obstruction was unable to be milled through. The obstruction has not at this stage been identified. At that stage and because the Baker Hughes cleaning fluids had already been delivered, could not be returned and had only a few days of effectiveness it was decided that the fluids be pumped into the well bore in any case in the hope that they would still have some effectiveness.

 

Following the pumping operation the well was allowed to clean up and was flowed at first to the flare pit before being turned back to the sales line.

 

Well production following the cleanout operation appears the same as before the cleanout with no real change.

 

The operator has formed the view that the obstruction is acting as a down hole choke and is limiting production. It is also likely that the cleanout fluids did not reach the desired zone to effectively cleanout the well bore as planned.

 

The operator plans to consult with a cased hole expert to determine the options to remove the obstruction. In the meantime the well is flowing to sales at rates averaging 500,000-600,000 cubic feet of gas per day.

 

The operator is optimistic that the obstruction can be located, sized and removed to allow an effective cleanout operation to proceed and enable improved flow rates to be achieved.

 

Further updates will be provided as appropriate.

 

 

The information contained in this announcement was reviewed by the Technical Director of Empyrean Energy Plc, Mr Frank Brophy BSc (Hons) who has over 40 years experience as a petroleum geologist.

 

Contact:

 

Empyrean Energy Plc

Tom Kelly

Tel: +618 9388 8041

 

 

Shore Capital

Anita Ghanekar

Edward Mansfield

Tel: +44 20 7408 4090

This information is provided by RNS
The company news service from the London Stock Exchange
 
END
 
 
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