RE: Risk?4 Dec 2021 09:00
Hey, cut the aggression eh? You are both wrong.
"In March 2021, pressure variability was observed in the P6 well while utilising the lower ESP, with subsequent investigations suggesting a potential partial obstruction to fluid flow above the lower ESP. Production was restored to prior rates after a well intervention which switched over to utilising the upper ESP in the well. Investigations are still ongoing into the root cause of this issue. Should the upper ESP in the P6 well fail in the future, there is a risk that the lower ESP cannot be restored to full function, in which case the Company might need to flow the well at lower rates."
Read RNS Number : 1528X. There has been zero news about the lower pump being brought back on line. Reverting to natural flow on P6 when the upper pump tripped in June strongly suggests the second, lower pump is still not available.