Less Ads, More Data, More Tools Register for FREE

Pin to quick picksSEY.L Regulatory News (SEY)

  • There is currently no data for SEY

Kurdistan Operations Update

6 Jul 2011 07:00

RNS Number : 8342J
Sterling Energy PLC
06 July 2011
 



 

6 July 2011

 

STERLING ENERGY PLC

("Sterling" or the "Company")

 

Kurdistan Operations Update

 

Sterling (AIM: SEY), the independent oil and gas exploration and production company with interests in the Middle East and Africa, provides the following update for the Sterling operated Sangaw North block in Kurdistan (53.33% working interest).

 

Flow testing operations have been completed in the cased hole section of the Sangaw North-1 well. Two flow tests were conducted; the first across a 100 metre interval within the Jurassic aged Sargelu formation and the second across a 100 metre interval within the Cretaceous aged Kometan formation.

 

During the first flow test, formation gas and water were observed in small quantities at surface but sustainable flow rates were not achieved. The Company believes that the Jurassic aged Sargelu formation does not contain a sufficient natural fracture network to support sustained flow.

 

During the second flow test, within the Cretaceous aged Kometan formation, the well flowed at a stabilised rate of approximately 0.4 million standard cubic feet of gas and 4,500 barrels of formation water per day during an 8 hour flow period through a 60/64ths inch choke with a wellhead pressure of 280 pounds per square inch. Approximately 83 per cent of the produced gas was hydrocarbon gas with the remainder comprising 10 per cent hydrogen sulphide and 7 per cent carbon dioxide.

 

Neither flow test produced hydrocarbons at commercial rates and the Sangaw North-1 well will now be plugged and abandoned. The operations to plug and abandon the well are expected to take approximately 2 weeks, after which the drilling rig will be demobilised from the location.

 

The current exploration phase of the Production Sharing Contract for the Sangaw North area will expire in November 2011 and the joint venture partnership (Sterling, Addax and KNOC) may elect to enter the next exploration phase which runs until November 2013; the Sangaw North-1 well has fulfilled the work commitment for this next phase. During the coming months Sterling will integrate and analyse the seismic, drilling, logging and testing data before making recommendations to the joint venture group.

 

Angus MacAskill, Sterling's Chief Executive said:

 

"We are disappointed that flow testing has not demonstrated commercial hydrocarbon flow rates in the Sangaw North-1 well. An integrated interpretation of all the data acquired during well operations will be conducted to determine the remaining potential of the Sangaw North structure prior to a decision on future operations."

 

 

Further information:

Sterling Energy plc

(+44 20 7405 4133)

Alastair Beardsall, Chairman

Angus MacAskill, Chief Executive

 

Evolution Securities

(+44 20 7071 4300)

Chris Sim

Neil Elliot

 

 

 

Angus MacAskill, M.Eng. Petroleum Engineering (1987), Chief Executive of Sterling Energy Plc, who has been involved in the oil industry for 29 years, is the qualified person that has reviewed the technical information contained in this press release.

This information is provided by RNS
The company news service from the London Stock Exchange
 
END
 
 
MSCBLGDRCSGBGBU
Date   Source Headline
11th Apr 20064:52 pmRNSHolding(s) in Company
3rd Apr 200610:41 amRNSNotice of Results
17th Mar 20062:42 pmRNSHolding(s) in Company
27th Feb 20067:03 amRNSFirst Oil Announcement
14th Feb 20062:25 pmRNSDirector/PDMR Shareholding
14th Feb 20067:00 amRNSBOARD APPOINTMENT
24th Jan 20067:00 amRNSDrilling Report
17th Jan 20067:00 amRNSDrilling Report
7th Dec 200510:12 amRNSAdditional Listing
7th Dec 20057:01 amRNSOperational Update
24th Nov 20057:00 amRNSAGM Presentation
22nd Nov 20057:00 amRNSDrilling Report
18th Nov 20057:00 amRNSDrilling Report
15th Nov 20057:00 amRNSDrilling Report
8th Nov 20057:02 amRNSDrilling Report
4th Nov 200511:08 amRNSAdditional Listing
1st Nov 20057:01 amRNSDrilling Report
28th Oct 20057:01 amRNSDrilling Report
25th Oct 20057:01 amRNSDrilling Report
18th Oct 20057:01 amRNSDrilling Report
11th Oct 20057:01 amRNSDrilling Report
30th Sep 20052:45 pmRNSHolding(s) in Company
30th Sep 200511:15 amRNSSale of Shares
27th Sep 20057:03 amRNSDrilling Report
26th Sep 20057:03 amRNSDrilling Report
23rd Sep 20057:00 amRNSInterim Results
20th Sep 20057:04 amRNSDrilling Report
14th Sep 20054:24 pmRNSNotice of Results
13th Sep 20057:04 amRNSDrilling Report
13th Sep 20057:01 amRNSActivity Update
6th Sep 20057:05 amRNSDrilling Report
5th Sep 200512:57 pmRNSHolding(s) in Company
30th Aug 20057:02 amRNSDrilling Report
24th Aug 20053:21 pmRNSHolding(s) in Company
24th Aug 20058:47 amRNSDrilling Report
16th Aug 20055:51 pmRNSDrilling Report
16th Aug 20057:00 amRNSDrilling Report
8th Aug 20057:00 amRNSDrilling Report
4th Aug 20058:00 amRNSMauritania
19th Jul 20057:00 amRNSMadagascar Farm-Out Deal
15th Jul 20057:01 amRNSClarification of Media Report
8th Jul 200511:12 amRNSHolding(s) in Company
29th Jun 200511:50 amRNSAGM Statement
29th Jun 20057:00 amRNSSuccessful Well Operations
22nd Jun 20055:34 pmRNSDrilling Report
7th Jun 20051:14 pmRNSDirector Shareholding
7th Jun 20057:11 amRNSChinguetti Finance Facility
2nd Jun 20051:38 pmRNSChinguetti Drilling Update
19th May 200511:04 amRNSDirector Shareholding
11th May 20057:00 amRNSFinal Results

Due to London Stock Exchange licensing terms, we stipulate that you must be a private investor. We apologise for the inconvenience.

To access our Live RNS you must confirm you are a private investor by using the button below.