RE: People posting negatively with intent26 Jan 2020 11:23
Suemay1 What a crazy comment to make, no wonder UKOG holders keep coming on here . Over 80,000 barrels of oil has flowed out of HH1 to date with not a barrel of water. UJO would love figures like that.
"Word is the main attraction at the Surrey NOT so fun park is closed. It Got flooded with water and theyve got no spare parts to fix it."
Adrian has gone through a lot these last 3 months. Big heart attack that could of killed him, then having your chest opened to do a Tripple Heart Bypass and all the mental worry that goes with that. I'm not surprised he expressed his frustration yesterday with UKOG. Well done Adrian, just hope you are not back on the booze and fags. In support of UKOG We know HH1 is producing and tankers are leaving the gates. We know HH2 has a water problem near the end of the well and it is going to be fixed as soon as equipment can be arranged. We know it has flowed and potentially can flow at a rate of 600 to 1000bopd At the moment it is on a Longterm PDU whilst equipment is mobilised. To date nearly 400 tankers of Kimmeridge and Portland oil has flowed from a small trial well producing 3 million + income.
RE: Tankers are still leaving.. twitter but no pics today24 Jan 2020 12:32
Steptoes Wealdoilers can only relay what he is told as he is in Spain at the moment and his lenses are not that long. He is also told that the pump is pumping over HH1 and the flare flaring. For the non believers go and have a look for yourselves.
Ninetails Shares are for buying and selling, sometime I hold for days, some times weeks and sometimes months but I do not hold for years. I do not pump and dump like Heid, Straighttalker, Coil etc but I do put up factual pictures / reports that I hope help other investors to decide whether to buy or sell. My Twitter heading says it all "Only invest what you can afford to lose, shares go up and down, information given is only in my opinion"
Kford The reason they stopped 500ft short was that the drill rig motor burnt out / caught fire and drilling had to stop till a new motor was put in. It took about 4 / 5 days to repair and then they decided not to drill any further.
Baits UjO have alot of expenditure over the next 12 months and they have no control of how it is spent, Rathlin are in charge. UKOG are in charge of expenditure. UJO only have a 27% interest against UKOG 86% UJO are flowing no oil from West newton A or B wells or Wressel UKOG have tankers leaving most days and generated approx 3 million of income already. UKOG have drilled HH2 and have small water problem which ukog say is easy to fix. HH2 flowed in the test the equivalent of 600bopd UJO have alot of catching up to do. UJO is still good for a trade now and then.
RE: PMTpiper, Zac Philips, the Oil analyst20 Jan 2020 08:33
Straighttalker You missed out the important word ESTIMATED constrained flow of 500 bopd Not sure how they are going to get an ESTIMATED 500bopd from a well that all 3 zones only flowed max 350 barrel of oil, the rest was gas flared of.